September 12, 2011
summary what was been done
Run # | Beam | Dump magnet | Collimator | Radiator 10 um Al | Target | Comments |
---|---|---|---|---|---|---|
2359 | Centered | In | Open | Out | No | Test radiator in/out.
R(upstream) = 157/40244 = 0.0039 e+/pulse, |
2360 | Centered | In | Open | Centered | No | Test radiator in/out.
R(upstream) = 898/40244 = 0.0223 e+/pulse, |
2361 | Up 2 mm | In | Open | Up 2 mm | No | Test radiator in/out.
R(upstream) = 730/40839 = 0.0179 e+/pulse, |
2362 | Up 2 mm | In | Open | Out | No | Test radiator in/out.
R(upstream) = 172/41035 = 0.0042 e+/pulse, |
2363 | Up 2 mm | In | Open | Out | No | Test radiator in/out. Added 1" Al hardener against Cu bricks after vacuum window.
R(upstream) = 87/41037 = 0.0021 e+/pulse, |
2364 | Up 2 mm | In | Open | Up 2 mm | No | Test radiator in/out.
R(upstream) = 777/50837 = 0.0153 e+/pulse, |
2365 | Up 2 mm | In | Open | Up 2 mm | No | Test radiator in/out. Now 2" Al hardener against Cu bricks after vacuum window.
R(upstream) = 574/41235 = 0.0139 e+/pulse, |
2366 | Up 2 mm | In | Open | Out | No | Test radiator in/out.
R(upstream) = 117/41035 = 0.0028 e+/pulse, |
2367 | Down 2 mm | In | Open | Out | No | Test radiator in/out. Removed 2" Al hardener
R(upstream) = 160/41036 = 0.0039 e+/pulse, |
2368 | Down 2 mm | In | Open | Down 2 mm | No | Test radiator in/out.
R(upstream) = 628/40639 = 0.0154 e+/pulse, |
2369 | Down 2 mm | In | Open | Down 2 mm | No | Test radiator in/out. Added 1" Al hardener against Cu bricks after vacuum window.
R(upstream) = 454/40640 = 0.0111 e+/pulse, |
2370 | Down 2 mm | In | Open | Out | No | Test radiator in/out.
R(upstream) = 98/40639 = 0.0024 e+/pulse, |
2371 | Up 2 mm | In | Open | Up 2 mm | No | Test radiator in/out to reproduce previous result. Same 1" Al hardener against Cu bricks after vacuum window.
R(upstream) = 935/40641 = 0.0230 e+/pulse, |
2372 | Up 2 mm | In | Open | Out | No | Test radiator in/out.
R(upstream) = 153/40640 = 0.0038 e+/pulse, |
2374 | Up 2 mm | In | Open | Up 2 mm | DU plate | DU plate oriented 45 and 45 degree. Same 1" Al hardener upstream of collimator.
Too short |
2375 | Up 2 mm | In | Open | Up 2 mm | DU plate | Same. Re-doing 2374
R(beam left) = 0.0003 n/pulse |
2376 | Up 2 mm | In | Open | Out | DU plate | R(beam left) = 0/176520 = 0 n/pulse R(beam right) = 0/176520 = 0 n/pulse About 83% of photons are coming from the radiator. Good |
2377 | Down 2 mm | In | Open | Out | DU plate | R(beam left) = 6/166815 = 0.0000359 n/pulse R(beam down) = 4/166815 = 0.0000239 n/pulse |
2378 | Down 2 mm | In | Open | Down 2 mm | DU plate | R(beam 45 left) = 0.000139 n/pulse R(beam down) = 174/238320 = 0.000730 n/pulse About 82% of photons are coming from the radiator. Good |
2379 | Down 2 mm | In | Open | Down 2 mm | DU plate | Increased voltage on 2 photonics (A22 & A24) detectors from -1600 -> -1700 V. Production run.
R(beam 45 left) = 285/600204 = 0.00047 n/pulse (A22) |
2380 | Down 2 mm | In | Open | Out | DU plate | Production run.
R(beam 45 left) = 1/216331 = 0.00000462 n/pulse |
2381 | Up 2 mm | In | Open | Out | DU plate | Production run.
R(beam 45 left) = 4/171170 = 0.0000234 n/pulse |
2382 | Up 2 mm | In | Open | Up 2 mm | DU plate | Production run.
R(beam 45 left) = 475/583758 = 0.00081 n/pulse |